ARM: dts: LogicPD Torpedo: Fix I2C1 pinmux

commit 74402055a2d3ec998a1ded599e86185a27d9bbf4 upstream.

The pinmuxing was missing for I2C1 which was causing intermittent issues
with the PMIC which is connected to I2C1.  The bootloader did not quite
configure the I2C1 either, so when running at 2.6MHz, it was generating
errors at time.

This correctly sets the I2C1 pinmuxing so it can operate at 2.6MHz

Fixes: 687c276761 ("ARM: dts: Add minimal support for LogicPD Torpedo
DM3730 devkit")

Signed-off-by: Adam Ford <aford173@gmail.com>
Signed-off-by: Tony Lindgren <tony@atomide.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
This commit is contained in:
Adam Ford 2018-01-25 14:10:37 -06:00 committed by Greg Kroah-Hartman
parent 036c4bdd66
commit 29b2031139

View file

@ -90,6 +90,8 @@
};
&i2c1 {
pinctrl-names = "default";
pinctrl-0 = <&i2c1_pins>;
clock-frequency = <2600000>;
twl: twl@48 {
@ -137,6 +139,12 @@
OMAP3_CORE1_IOPAD(0x218e, PIN_OUTPUT | MUX_MODE4) /* mcbsp1_fsr.gpio_157 */
>;
};
i2c1_pins: pinmux_i2c1_pins {
pinctrl-single,pins = <
OMAP3_CORE1_IOPAD(0x21ba, PIN_INPUT | MUX_MODE0) /* i2c1_scl.i2c1_scl */
OMAP3_CORE1_IOPAD(0x21bc, PIN_INPUT | MUX_MODE0) /* i2c1_sda.i2c1_sda */
>;
};
};
&omap3_pmx_core2 {