An incorrect ordering in the error checking code lead
to DP aux defer being skipped in the aux native write
path. Move the bytes transferred check (ret == 0)
below the defer check.
Tracked down by: Brad Campbell <brad@fnarfbargle.com>
Fixes:
https://bugs.freedesktop.org/show_bug.cgi?id=41121
Signed-off-by: Alex Deucher <alexander.deucher@amd.com>
Cc: Brad Campbell <brad@fnarfbargle.com>
Cc: stable@kernel.org
Signed-off-by: Dave Airlie <airlied@redhat.com>
GRE connections cause ctnetlink event flood because the ASSURED event
is set for every packet received.
Reported-by: Denys Fedoryshchenko <denys@visp.net.lb>
Tested-by: Denys Fedoryshchenko <denys@visp.net.lb>
Signed-off-by: Florian Westphal <fw@strlen.de>
Signed-off-by: Pablo Neira Ayuso <pablo@netfilter.org>
omap_mcpdm_remove is used from asoc_mcpdm_probe, which is an
initcall, and must not be discarded when HOTPLUG is disabled.
Signed-off-by: Arnd Bergmann <arnd@arndb.de>
Signed-off-by: Mark Brown <broonie@opensource.wolfsonmicro.com>
Current code set update bits for WM8753_LDAC and WM8753_RDAC twice,
but missed setting update bits for WM8753_LADC and WM8753_RADC.
I think it is a copy-paste bug in commit 776065
"ASoC: codecs: wm8753: Fix register cache incoherency".
Signed-off-by: Axel Lin <axel.lin@gmail.com>
Signed-off-by: Mark Brown <broonie@opensource.wolfsonmicro.com>
Cc: stable@kernel.org
A recent conversion has introduced references to &pdev->dev, which does
not actually exist in all the contexts it's used in.
Replace this with card->dev where necessary, in order to let
the driver build again.
Signed-off-by: Arnd Bergmann <arnd@arndb.de>
Signed-off-by: Mark Brown <broonie@opensource.wolfsonmicro.com>
Cc: stable@kernel.org
I hit a crash in qla2x00_abort_all_cmds() if the qla2xxx module is
unloaded right after it is loaded. I debugged this down to the abort
handling improperly treating a command of type SRB_ADISC_CMD as if it
had a bsg_job to complete when that command actually uses the iocb_cmd
part of the union. (I guess to hit this one has to unload the module
while the async FC initialization is still in progress)
It seems we should only look for a bsg_job if type is SRB_ELS_CMD_RPT,
SRB_ELS_CMD_HST or SRB_CT_CMD, so switch the test to make that explicit.
Signed-off-by: Roland Dreier <roland@purestorage.com>
Acked-by: Chad Dupuis <chad.dupuis@qlogic.com>
Cc: stable@kernel.org
Signed-off-by: James Bottomley <JBottomley@Parallels.com>
The CONFIG_ARM_AMBA symbol is selected by the platforms that support
AMBA, and the other platforms (e.g. orion) might not be able to
build that code at all when they do not support the clk API.
Instead, make sure that OC_ETM is only built on platforms that
do support the amba subsystem already.
Signed-off-by: Arnd Bergmann <arnd@arndb.de>
Some PCI drivers call pcibios_bus_to_resource directly,
but it is only exported when CONFIG_HOTPLUG is set,
because it was initially mean for pccard support.
Moving the export out of the #ifdef lets us avoid these
build errors:
ERROR: "pcibios_bus_to_resource" [drivers/video/vt8623fb.ko] undefined!
ERROR: "pcibios_bus_to_resource" [drivers/video/arkfb.ko] undefined!
ERROR: "pcibios_bus_to_resource" [drivers/video/s3fb.ko] undefined!
Signed-off-by: Arnd Bergmann <arnd@arndb.de>
These functions are used in some PCI drivers with big-endian
MMIO space, and they are trivial to add here.
Signed-off-by: Arnd Bergmann <arnd@arndb.de>
Support for IDE drivers should not be automatic, since most platforms
cannot actually support any IDE low-level drivers. This partly
reverts 2064c946e "ARM: always select HAVE_IDE" to set this symbol
only when either a PC-style bus (PCI, ISA, PCMCIA) is enabled or
a platform is used that is known to have an existing driver in
drivers/ide.
New platforms should not need this option and just use CONFIG_ATA
with drivers/ata/.
Signed-off-by: Arnd Bergmann <arnd@arndb.de>
Support for the cpu_suspend functions is only built-in
when CONFIG_PM_SLEEP is enabled, but omap3/4, exynos4
and pxa always call cpu_suspend when CONFIG_PM is enabled.
Signed-off-by: Arnd Bergmann <arnd@arndb.de>
Distros are starting to ship with toolchains defaulting to
hardfloat. Using such a compiler to build the kernel fails
in the VFP directory with
arch/arm/vfp/entry.S:1:0: sorry, unimplemented: -mfloat-abi=hard and VFP
Adding -mfloat-abi=soft to the gcc command line fixes this.
Signed-off-by: Arnd Bergmann <arnd@arndb.de>
The two functions cpu_is_v6_unaligned and safe_usermode
are only defined when CONFIG_PROC_FS is enabled, but
are used outside of the #ifdef.
Signed-off-by: Arnd Bergmann <arnd@arndb.de>
Cc: Dave Martin <dave.martin@linaro.org>
Thumb2 kernels cannot be built with frame pointers, but can use the
ARM_UNWIND feature for unwinding instead. This makes sure that all
features that rely on unwinding includeing CONFIG_LATENCYTOP and
FAULT_INJECTION_STACKTRACE_FILTER do not enable frame pointers
when the unwinder is already selected, and we always build with
the unwinder when we want a thumb2 kernel, to make sure we do not
get the frame pointers instead.
A different option would be to redefine the CONFIG_FRAME_POINTERS
option on ARM to mean builing with either frame pointers or
the unwinder, and then select which one to use based on the
CPU architecture or another user option. That would still allow
building thumb2 kernels without the unwinder but would also be
more confusing.
Signed-off-by: Arnd Bergmann <arnd@arndb.de>
The SMP implementation on ARM heavily depends on MMU-only code.
As long as nobody is interested in fixing this, let's disable the
SMP option when building for nommu.
Signed-off-by: Arnd Bergmann <arnd@arndb.de>
The rtc_lock is used by both the nvram and rtc drivers, so
we need to export it if at least one of the two is built,
not just for the rtc driver.
Signed-off-by: Arnd Bergmann <arnd@arndb.de>
The VM subsystem assumes that there are valid memmap entries from
the bank start aligned to MAX_ORDER_NR_PAGES.
On the Ux500 we have a lot of mem=N arguments on the commandline
triggering this bug several times over and causing kernel
oops messages.
Cc: stable@kernel.org
Cc: Michael Bohan <mbohan@codeaurora.org>
Cc: Nicolas Pitre <nico@fluxnic.net>
Signed-off-by: Johan Palsson <johan.palsson@stericsson.com>
Signed-off-by: Rabin Vincent <rabin.vincent@stericsson.com>
Signed-off-by: Linus Walleij <linus.walleij@linaro.org>
Signed-off-by: Russell King <rmk+kernel@arm.linux.org.uk>
* 'irq-urgent-for-linus' of git://tesla.tglx.de/git/linux-2.6-tip:
irq: Fix check for already initialized irq_domain in irq_domain_add
irq: Add declaration of irq_domain_simple_ops to irqdomain.h
* 'x86-urgent-for-linus' of git://tesla.tglx.de/git/linux-2.6-tip:
x86/rtc: Don't recursively acquire rtc_lock
* 'sched-urgent-for-linus' of git://tesla.tglx.de/git/linux-2.6-tip:
posix-cpu-timers: Cure SMP wobbles
sched: Fix up wchan borkage
sched/rt: Migrate equal priority tasks to available CPUs
A user reported a problem where ceph was getting into 100% cpu usage while doing
some writing. It turns out it's because we were doing a short write on a not
uptodate page, which means we'd fall back at one page at a time and fault the
page in. The problem is our position is on the page boundary, so our fault in
logic wasn't actually reading the page, so we'd just spin forever or until the
page got read in by somebody else. This will force a readpage if we end up
doing a short copy. Alexandre could reproduce this easily with ceph and reports
it fixes his problem. I also wrote a reproducer that no longer hangs my box
with this patch. Thanks,
Reported-and-tested-by: Alexandre Oliva <aoliva@redhat.com>
Signed-off-by: Josef Bacik <josef@redhat.com>
Signed-off-by: Chris Mason <chris.mason@oracle.com>
Current code calls omap4430_phy_init() twice in usb_musb_init().
Calling omap4430_phy_init() once is enough.
This patch removes the first omap4430_phy_init() call, which using an
uninitialized pointer as parameter.
This patch elimates below build warning:
arch/arm/mach-omap2/usb-musb.c: In function 'usb_musb_init':
arch/arm/mach-omap2/usb-musb.c:141: warning: 'dev' may be used uninitialized in this function
Signed-off-by: Axel Lin <axel.lin@gmail.com>
Bjarne Steinsbo <bsteinsbo@gmail.com>
Acked-by: Felipe Balbi <balbi@ti.com>
Signed-off-by: Tony Lindgren <tony@atomide.com>
Looks like 2600 kHz rate does not work reliably on 2430,
so just use the 100 kHz rate.
Otherwise the system often fails to boot properly with:
omap_i2c omap_i2c.2: timeout waiting for bus ready
omap_i2c omap_i2c.2: timeout waiting for bus ready
twl: i2c_write failed to transfer all messages
omap_i2c omap_i2c.2: timeout waiting for bus ready
twl: i2c_write failed to transfer all messages
omap_i2c omap_i2c.2: timeout waiting for bus ready
twl: i2c_write failed to transfer all messages
twl: clock init err [-110]
omap_i2c omap_i2c.2: timeout waiting for bus ready
twl: i2c_write failed to transfer all messages
TWL4030 Unable to unlock IDCODE registers --110
Signed-off-by: Tony Lindgren <tony@atomide.com>
Remove OMAP4_USBC1_ICUSB_PWRDNZ_MASK during enable/disable PWRDNZ mode for
MMC1_PBIAS and associated extended-drain MMC1 I/O cell. This is in accordance
with the control module programming guide. This fixes a bug where if trying to
use gpio_98 or gpio_99 and MMC1 at the same time the GPIO signal will be
affected by a changing SDMMC1_VDDS.
Software must keep MMC1_PBIAS cell and MMC1_IO cell PWRDNZ signals low whenever
SDMMC1_VDDS ramps up/down or changes for cell protection purposes.
MMC1 is based on SDMMC1_VDDS whereas USBC1 is based on SIM_VDDS therefore
they can operate independently.
Signed-off-by: Bryan Buckley <bryan.buckley@ti.com>
Acked-by: Kishore Kadiyala <kishore.kadiyala@ti.com>
Tested-by: Balaji T K <balajitk@ti.com>
Signed-off-by: Tony Lindgren <tony@atomide.com>
David reported:
Attached below is a watered-down version of rt/tst-cpuclock2.c from
GLIBC. Just build it with "gcc -o test test.c -lpthread -lrt" or
similar.
Run it several times, and you will see cases where the main thread
will measure a process clock difference before and after the nanosleep
which is smaller than the cpu-burner thread's individual thread clock
difference. This doesn't make any sense since the cpu-burner thread
is part of the top-level process's thread group.
I've reproduced this on both x86-64 and sparc64 (using both 32-bit and
64-bit binaries).
For example:
[davem@boricha build-x86_64-linux]$ ./test
process: before(0.001221967) after(0.498624371) diff(497402404)
thread: before(0.000081692) after(0.498316431) diff(498234739)
self: before(0.001223521) after(0.001240219) diff(16698)
[davem@boricha build-x86_64-linux]$
The diff of 'process' should always be >= the diff of 'thread'.
I make sure to wrap the 'thread' clock measurements the most tightly
around the nanosleep() call, and that the 'process' clock measurements
are the outer-most ones.
---
#include <unistd.h>
#include <stdio.h>
#include <stdlib.h>
#include <time.h>
#include <fcntl.h>
#include <string.h>
#include <errno.h>
#include <pthread.h>
static pthread_barrier_t barrier;
static void *chew_cpu(void *arg)
{
pthread_barrier_wait(&barrier);
while (1)
__asm__ __volatile__("" : : : "memory");
return NULL;
}
int main(void)
{
clockid_t process_clock, my_thread_clock, th_clock;
struct timespec process_before, process_after;
struct timespec me_before, me_after;
struct timespec th_before, th_after;
struct timespec sleeptime;
unsigned long diff;
pthread_t th;
int err;
err = clock_getcpuclockid(0, &process_clock);
if (err)
return 1;
err = pthread_getcpuclockid(pthread_self(), &my_thread_clock);
if (err)
return 1;
pthread_barrier_init(&barrier, NULL, 2);
err = pthread_create(&th, NULL, chew_cpu, NULL);
if (err)
return 1;
err = pthread_getcpuclockid(th, &th_clock);
if (err)
return 1;
pthread_barrier_wait(&barrier);
err = clock_gettime(process_clock, &process_before);
if (err)
return 1;
err = clock_gettime(my_thread_clock, &me_before);
if (err)
return 1;
err = clock_gettime(th_clock, &th_before);
if (err)
return 1;
sleeptime.tv_sec = 0;
sleeptime.tv_nsec = 500000000;
nanosleep(&sleeptime, NULL);
err = clock_gettime(th_clock, &th_after);
if (err)
return 1;
err = clock_gettime(my_thread_clock, &me_after);
if (err)
return 1;
err = clock_gettime(process_clock, &process_after);
if (err)
return 1;
diff = process_after.tv_nsec - process_before.tv_nsec;
printf("process: before(%lu.%.9lu) after(%lu.%.9lu) diff(%lu)\n",
process_before.tv_sec, process_before.tv_nsec,
process_after.tv_sec, process_after.tv_nsec, diff);
diff = th_after.tv_nsec - th_before.tv_nsec;
printf("thread: before(%lu.%.9lu) after(%lu.%.9lu) diff(%lu)\n",
th_before.tv_sec, th_before.tv_nsec,
th_after.tv_sec, th_after.tv_nsec, diff);
diff = me_after.tv_nsec - me_before.tv_nsec;
printf("self: before(%lu.%.9lu) after(%lu.%.9lu) diff(%lu)\n",
me_before.tv_sec, me_before.tv_nsec,
me_after.tv_sec, me_after.tv_nsec, diff);
return 0;
}
This is due to us using p->se.sum_exec_runtime in
thread_group_cputime() where we iterate the thread group and sum all
data. This does not take time since the last schedule operation (tick
or otherwise) into account. We can cure this by using
task_sched_runtime() at the cost of having to take locks.
This also means we can (and must) do away with
thread_group_sched_runtime() since the modified thread_group_cputime()
is now more accurate and would deadlock when called from
thread_group_sched_runtime().
Aside of that it makes the function safe on 32 bit systems. The old
code added t->se.sum_exec_runtime unprotected. sum_exec_runtime is a
64bit value and could be changed on another cpu at the same time.
Reported-by: David Miller <davem@davemloft.net>
Signed-off-by: Peter Zijlstra <a.p.zijlstra@chello.nl>
Cc: stable@kernel.org
Link: http://lkml.kernel.org/r/1314874459.7945.22.camel@twins
Tested-by: David Miller <davem@davemloft.net>
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
The commit a810364a04
ALSA: hda - Handle -1 as invalid position, too
caused a regression on some machines that require the position-buffer
instead of LPIB, e.g. resulting in noises with mic recording with
PulseAudio.
This patch fixes the detection by delaying the test at the timing as
same as 3.0, i.e. doing the position check only when requested in
azx_position_ok().
Reported-and-tested-by: Rocko Requin <rockorequin@hotmail.com>
Signed-off-by: Takashi Iwai <tiwai@suse.de>
__find_resource() incorrectly returns a resource window which overlaps
an existing allocated window. This happens when the parent's
resource-window spans 0x00000000 to 0xffffffff and is entirely allocated
to all its children resource-windows.
__find_resource() looks for gaps in resource allocation among the
children resource windows. When it encounters the last child window it
blindly tries the range next to one allocated to the last child. Since
the last child's window ends at 0xffffffff the calculation overflows,
leading the algorithm to believe that any window in the range 0x0000000
to 0xfffffff is available for allocation. This leads to a conflicting
window allocation.
Michal Ludvig reported this issue seen on his platform. The following
patch fixes the problem and has been verified by Michal. I believe this
bug has been there for ages. It got exposed by git commit 2bbc694227
("PCI : ability to relocate assigned pci-resources")
Signed-off-by: Ram Pai <linuxram@us.ibm.com>
Tested-by: Michal Ludvig <mludvig@logix.net.nz>
Signed-off-by: Linus Torvalds <torvalds@linux-foundation.org>
* 'v4l_for_linus' of git://linuxtv.org/mchehab/for_linus:
[media] omap3isp: Fix build error in ispccdc.c
[media] uvcvideo: Fix crash when linking entities
[media] v4l: Make sure we hold a reference to the v4l2_device before using it
[media] v4l: Fix use-after-free case in v4l2_device_release
[media] uvcvideo: Set alternate setting 0 on resume if the bus has been reset
[media] OMAP_VOUT: Fix build break caused by update_mode removal in DSS2
* 'for-linus' of git://git390.marist.edu/pub/scm/linux-2.6:
[S390] cio: fix cio_tpi ignoring adapter interrupts
[S390] gmap: always up mmap_sem properly
[S390] Do not clobber personality flags on exec
* git://github.com/davem330/sparc:
sparc64: Force the execute bit in OpenFirmware's translation entries.
sparc: Make '-p' boot option meaningful again.
sparc, exec: remove redundant addr_limit assignment
sparc64: Future proof Niagara cpu detection.
* 'drm-intel-fixes' of git://people.freedesktop.org/~keithp/linux:
drm/i915: FBC off for ironlake and older, otherwise on by default
drm/i915: Enable SDVO hotplug interrupts for HDMI and DVI
drm/i915: Enable dither whenever display bpc < frame buffer bpc
Apple Quad G5 has some oddity in it's device-tree which causes the new
generic matching code to fail to relate nodes for PCI-E devices below U4
with their respective struct pci_dev. This breaks graphics on those
machines among others.
This fixes it using a quirk which copies the node pointer from the host
bridge for the root complex, which makes the generic code work for the
children afterward.
Signed-off-by: Benjamin Herrenschmidt <benh@kernel.crashing.org>
Signed-off-by: Linus Torvalds <torvalds@linux-foundation.org>
Commit d5767c5353 ("bootup: move 'usermodehelper_enable()' to the end
of do_basic_setup()") moved 'usermodehelper_enable()' to end of
do_basic_setup() to after the initcalls. But then I get failed to let
uvesafb work on my computer, and lose the splash boot.
So maybe we could start usermodehelper_enable a little early to make
some task work that need eary init with the help of user mode.
[ I would *really* prefer that initcalls not call into user space - even
the real 'init' hasn't been execve'd yet, after all! But for uvesafb
it really does look like we don't have much choice.
I considered doing this when we mount the root filesystem, but
depending on config options that is in multiple places. We could do
the usermode helper enable as a rootfs_initcall()..
So I'm just using wang yanqing's trivial patch. It's not wonderful,
but it's simple and should work. We should revisit this some day,
though. - Linus ]
Signed-off-by: Linus Torvalds <torvalds@linux-foundation.org>
The commit aabdcb0b55 ("can bcm: fix tx_setup
off-by-one errors") fixed only a part of the original problem reported by
Andre Naujoks. It turned out that the original code needed to be re-ordered
to reduce complexity and to finally fix the reported frame counting issues.
Signed-off-by: Oliver Hartkopp <socketcan@hartkopp.net>
Signed-off-by: David S. Miller <davem@davemloft.net>
Wrong pointer is being passed for raw data sanity checking, when parsing
sample event.
This ends up with invalid event and perf record being stuck in
__perf_session__process_events function during processing build IDs
(process_buildids function).
Following command hangs up in my setup:
./perf record -e raw_syscalls:sys_enter ls
The fix is to use proper pointer to the raw data instead of the 'u'
union.
Reviewed-by: David Ahern <dsahern@gmail.com>
Cc: David Ahern <dsahern@gmail.com>
Cc: Eric Dumazet <eric.dumazet@gmail.com>
Cc: Ingo Molnar <mingo@elte.hu>
Cc: Neil Horman <nhorman@tuxdriver.com>
Cc: Paul Mackerras <paulus@samba.org>
Cc: Peter Zijlstra <a.p.zijlstra@chello.nl>
Cc: Steven Rostedt <rostedt@goodmis.org>
Link: http://lkml.kernel.org/r/1317308709-9474-2-git-send-email-jolsa@redhat.com
Signed-off-by: Jiri Olsa <jolsa@redhat.com>
Signed-off-by: Arnaldo Carvalho de Melo <acme@redhat.com>
In the OF 'translations' property, the template TTEs in the mappings
never specify the executable bit. This is the case even though some
of these mappings are for OF's code segment.
Therefore, we need to force the execute bit on in every mapping.
This problem can only really trigger on Niagara/sun4v machines and the
history behind this is a little complicated.
Previous to sun4v, the sun4u TTE entries lacked a hardware execute
permission bit. So OF didn't have to ever worry about setting
anything to handle executable pages. Any valid TTE loaded into the
I-TLB would be respected by the chip.
But sun4v Niagara chips have a real hardware enforced executable bit
in their TTEs. So it has to be set or else the I-TLB throws an
instruction access exception with type code 6 (protection violation).
We've been extremely fortunate to not get bitten by this in the past.
The best I can tell is that the OF's mappings for it's executable code
were mapped using permanent locked mappings on sun4v in the past.
Therefore, the fact that we didn't have the exec bit set in the OF
translations we would use did not matter in practice.
Thanks to Greg Onufer for helping me track this down.
Signed-off-by: David S. Miller <davem@davemloft.net>
In the rds_iw_mr_pool struct the free_pinned field keeps track of
memory pinned by free MRs. While this field is incremented properly
upon allocation, it is never decremented upon unmapping. This would
cause the rds_rdma module to crash the kernel upon unloading, by
triggering the BUG_ON in the rds_iw_destroy_mr_pool function.
This change keeps track of the MRs that become unpinned, so that
free_pinned can be decremented appropriately.
Signed-off-by: Jonathan Lallinger <jonathan@ogc.us>
Signed-off-by: Steve Wise <swise@ogc.us>
Signed-off-by: David S. Miller <davem@davemloft.net>
In xen_memory_setup() all reserved regions and gaps are set to an
identity (1-1) p2m mapping. If an available page has a PFN within one
of these 1-1 mappings it will become inaccessible (as it MFN is lost)
so release them before setting up the mapping.
This can make an additional 256 MiB or more of RAM available
(depending on the size of the reserved regions in the memory map) if
the initial pages overlap with reserved regions.
The 1:1 p2m mappings are also extended to cover partial pages. This
fixes an issue with (for example) systems with a BIOS that puts the
DMI tables in a reserved region that begins on a non-page boundary.
Signed-off-by: David Vrabel <david.vrabel@citrix.com>
Signed-off-by: Konrad Rzeszutek Wilk <konrad.wilk@oracle.com>
Allow the extra memory (used by the balloon driver) to be in multiple
regions (typically two regions, one for low memory and one for high
memory). This allows the balloon driver to increase the number of
available low pages (if the initial number if pages is small).
As a side effect, the algorithm for building the e820 memory map is
simpler and more obviously correct as the map supplied by the
hypervisor is (almost) used as is (in particular, all reserved regions
and gaps are preserved). Only RAM regions are altered and RAM regions
above max_pfn + extra_pages are marked as unused (the region is split
in two if necessary).
Signed-off-by: David Vrabel <david.vrabel@citrix.com>
Signed-off-by: Konrad Rzeszutek Wilk <konrad.wilk@oracle.com>
Allow the xen balloon driver to populate its list of extra pages from
more than one region of memory. This will allow platforms to provide
(for example) a region of low memory and a region of high memory.
The maximum possible number of extra regions is 128 (== E820MAX) which
is quite large so xen_extra_mem is placed in __initdata. This is safe
as both xen_memory_setup() and balloon_init() are in __init.
The balloon regions themselves are not altered (i.e., there is still
only the one region).
Signed-off-by: David Vrabel <david.vrabel@citrix.com>
Signed-off-by: Konrad Rzeszutek Wilk <konrad.wilk@oracle.com>
When initializing the balloon only max_pfn needs to be checked
(max_pfn will always be <= e820_end_of_ram_pfn()) and improve the
confusing comment.
Signed-off-by: David Vrabel <david.vrabel@citrix.com>
Signed-off-by: Konrad Rzeszutek Wilk <konrad.wilk@oracle.com>